sad story
Posted: Sun Jan 26, 2003 1:52 pm
hi
i havent been on for a few months, thought id bring you up to date - about a month before xmas, i noticed the ignition light on my 66 2 door saloon was taking longer and longer to go out, i measured the voltage coming off the dynamo at only about one volt, im sure i did it right (short the 2 terminals together - then measure between that and the earth ) - anyway rather than messing with it i ordered a replacement from ESM - while i was waiting, i had to get out so i thought ill take a spare battery and even if the dynamo isnt charging i'll run it until it stops then change the battery to get home - anyway then the oil light came on, no prob, i already had the oil and the filter element, it had done about 10k so i took it home, changed the oil and it all seemed to be fine (isnt it difficult to see fresh oil on a dipstick ?) - so off i went again with the spare battery - and it was going nice for about five miles, then i noticed the tapping noise which it had since i bought it was getting louder - i stopped and the engine was sounding like a big lawn mower with something stuck in it by now, and it was boiling up all over the place - i had to get it home so i let it cool off and drove it back - the noise was incredible by the time i got home - so that was that - i was already counting on spending a grand to get a lot of work done on the body (rotten boot, spring hangers,doors inner wings etc) to get it through its mot next month - well to get someone to take the engine apart was going to add a few more hundred including repairs to the engine compartment - it had had it !! oh no !! - anyway its sat there all xmas, ive now bought a traveller for 2 grand which isnt perfect but it is beautiful and its engine sounds like a bmw compared to my 2 door (even before it died) - i worked out the cost of all the spare parts from the 2 door that would be useful on the traveller and its getting on for 500 quids worth, 'll scrap the shell - yesterday i went and started the 2 door up after a month and its still going great except for that racket
cheers
grainger
i havent been on for a few months, thought id bring you up to date - about a month before xmas, i noticed the ignition light on my 66 2 door saloon was taking longer and longer to go out, i measured the voltage coming off the dynamo at only about one volt, im sure i did it right (short the 2 terminals together - then measure between that and the earth ) - anyway rather than messing with it i ordered a replacement from ESM - while i was waiting, i had to get out so i thought ill take a spare battery and even if the dynamo isnt charging i'll run it until it stops then change the battery to get home - anyway then the oil light came on, no prob, i already had the oil and the filter element, it had done about 10k so i took it home, changed the oil and it all seemed to be fine (isnt it difficult to see fresh oil on a dipstick ?) - so off i went again with the spare battery - and it was going nice for about five miles, then i noticed the tapping noise which it had since i bought it was getting louder - i stopped and the engine was sounding like a big lawn mower with something stuck in it by now, and it was boiling up all over the place - i had to get it home so i let it cool off and drove it back - the noise was incredible by the time i got home - so that was that - i was already counting on spending a grand to get a lot of work done on the body (rotten boot, spring hangers,doors inner wings etc) to get it through its mot next month - well to get someone to take the engine apart was going to add a few more hundred including repairs to the engine compartment - it had had it !! oh no !! - anyway its sat there all xmas, ive now bought a traveller for 2 grand which isnt perfect but it is beautiful and its engine sounds like a bmw compared to my 2 door (even before it died) - i worked out the cost of all the spare parts from the 2 door that would be useful on the traveller and its getting on for 500 quids worth, 'll scrap the shell - yesterday i went and started the 2 door up after a month and its still going great except for that racket
cheers
grainger