well i put a volt meter on it and it was reading 1.3
turned the revs up a bit more and 1.7
me thinks there's a problem lol
at least it's running right now.
checked timing ok
turned out to be throttle linkage filthy dirty and not going back properly and a dirty dash pot piston too.
good clean up and woo hoo lovely tick over even with a hot rod exhaust
it'll sound nice when i get the new one on lol
also sorted out the wiring prob it was the fan had been wired into the voltage regulator so overworking it after a few minutes.
re-wired and checked everything and hey presto fuel gauge reading nearly half (should be about right) and heater blowing nicely
isn't it lovely when you figure out whats wrong

and mend it