Help with Hif carb fitted to a+ 1300cc engine Please
Posted: Fri Jun 23, 2006 10:19 am
Hi all.
My First post for a while.And its a long one,sorry.
My mates pickup is coming on very well.
We have fitted the sierra 5 speed box and the rebuilt a+ Ital engine.
We have fitted the engine with a 3 branch exhuast and a water heated inlet manifold.
The car has an electric fuel pump as per standered.
I have made a breather with a small k+n filter for better breathing which is fitted to were the mechanical fuel pump blank would of been.
The front timing case has also got the modified breather cylinder and the rubber pipe is conected to the relevent fitting on the carb.
The carb fitted is a Ital hif type off the same original engine..
Having conected the fuel line from the pump/breather and the advance and retard vacume.
There appears to be a spare fuel connection/pipe? which we don't know wether it is a return pipe of some sort or vent.Or a return to the original air pan?(we do not have the original air filter set up)
We have an after market K+N style filter fitted
We have checked with the Haynes SU carb manual and we are none of the wiser as to what to do with this extra pipe or vent..
The carb is marked on the body JTX and also marked Pd c1.There is no identity tag on the carb.
We tested the fuel pump was working and the fuel itself started to come out of this pipe or vent?.We then blocked it off with a tube with a bolt inside before we carried on any further.
The problem we have is when we started the engine up it ran fine if you kept the revs higher than tickover but would cut out if left alone .It revved up and down great but seemed very sooty at the exhaust until we let it idle.
The next thing while we were setting the tick over ,the fuel started leaking out of the throttle body at the filter end ,onto the 3 branch.
We then very quickly turned it off and diconnected the battery and fuel pump wire.
We are not entirely sure what the problem is and that there may be something missing from the carburreters original airpan or something.
We then took the carb off and checked the needle valve was working by blowing down the fuel pipe connection and turning it upside down and it seems to be working fine.But this still could have an incorrect float setting i know .
Could it be the k+n airfilters rubber gasket be causing the problem?As there are holes around the mouth of the carb which are being bloked by the k+n style filters rubber gasket?I do not mean the mounting bolt holes.
Im sticking to welding and grinding for a while i think.
Any help and advice as to what could be the problem would be great and very appriciated..
I will add a few pictures in my next post so you have an idea of what i am talking about thanks ,Tim.
My First post for a while.And its a long one,sorry.
My mates pickup is coming on very well.
We have fitted the sierra 5 speed box and the rebuilt a+ Ital engine.
We have fitted the engine with a 3 branch exhuast and a water heated inlet manifold.
The car has an electric fuel pump as per standered.
I have made a breather with a small k+n filter for better breathing which is fitted to were the mechanical fuel pump blank would of been.
The front timing case has also got the modified breather cylinder and the rubber pipe is conected to the relevent fitting on the carb.
The carb fitted is a Ital hif type off the same original engine..
Having conected the fuel line from the pump/breather and the advance and retard vacume.
There appears to be a spare fuel connection/pipe? which we don't know wether it is a return pipe of some sort or vent.Or a return to the original air pan?(we do not have the original air filter set up)
We have an after market K+N style filter fitted
We have checked with the Haynes SU carb manual and we are none of the wiser as to what to do with this extra pipe or vent..
The carb is marked on the body JTX and also marked Pd c1.There is no identity tag on the carb.
We tested the fuel pump was working and the fuel itself started to come out of this pipe or vent?.We then blocked it off with a tube with a bolt inside before we carried on any further.
The problem we have is when we started the engine up it ran fine if you kept the revs higher than tickover but would cut out if left alone .It revved up and down great but seemed very sooty at the exhaust until we let it idle.
The next thing while we were setting the tick over ,the fuel started leaking out of the throttle body at the filter end ,onto the 3 branch.
We then very quickly turned it off and diconnected the battery and fuel pump wire.
We are not entirely sure what the problem is and that there may be something missing from the carburreters original airpan or something.
We then took the carb off and checked the needle valve was working by blowing down the fuel pipe connection and turning it upside down and it seems to be working fine.But this still could have an incorrect float setting i know .
Could it be the k+n airfilters rubber gasket be causing the problem?As there are holes around the mouth of the carb which are being bloked by the k+n style filters rubber gasket?I do not mean the mounting bolt holes.
Im sticking to welding and grinding for a while i think.
Any help and advice as to what could be the problem would be great and very appriciated..
I will add a few pictures in my next post so you have an idea of what i am talking about thanks ,Tim.