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Posted: Mon Jun 26, 2006 1:22 pm
by dunketh
Maybe the last head fitter forgot to re-tighten them after time. Its easily done I guess.
Oddly my rocker gasket has started leaking oil for no reason whatsoever - and its a new one.
I blame the weather, in true british style!
Posted: Mon Jun 26, 2006 1:33 pm
by Kevin
Yes your are probably right, I guess the same monkey that bodged the bypass tube.
Posted: Mon Jun 26, 2006 2:09 pm
by chrisd87
That's rather uncanny - my bypass hose sprang a leak just after I had the head off a few days ago. Got a couple of new ones - 95p from the local MG Rover dealer!

Posted: Mon Jun 26, 2006 2:45 pm
by Kevin
Got a couple of new ones - 95p from the local MG Rover dealer
Use a piece of heater hose its what was used originally and lasts far far longer than the bellows type. and I wish it was just the bypass hose that was my problem rather than the bypass tube .
Posted: Mon Jun 26, 2006 2:49 pm
by chrisd87
I would have used a piece of heater hose if I'd known it was dodgy when I had the head off, but only when I'd put it back on did it start leaking

Posted: Mon Jun 26, 2006 4:32 pm
by Kevin
Remember you dont have to take the head off to remove the hose just the water pump.
Posted: Tue Jun 27, 2006 12:26 pm
by dunketh
Bypass tube?
Do you mean the outlet the bypass hose attaches to?
If so can't you just stick a piece of copper pipe or suchlike in the whole with some JB Weld?
Might need to open the hole out a bit but thats all.
Posted: Tue Jun 27, 2006 11:46 pm
by Kevin
Bypass tube?
Do you mean the outlet the bypass hose attaches to?
Yes thats it on the underside of the head.
Hmm sorry but that sounds a bit of a bodge to me.
It might be ok as an emergency fix but with whats left of mine which is just a rusty serrated piece less than a third of its original length, I would rather it was done properly and what probably caused it was not running with a decent antifreeze mixture all year round some time in the past.
Posted: Wed Jun 28, 2006 8:31 am
by chickenjohn
Leaving the egg jokes aside (didn't Leonard Lord describe the Morris Minor as looking like a poached egg???)- back to head gaskets-
after doing a blown exhaust valve in Jan, the traveller ran very well but some oil crept into the water and a small amount of mayonnaise on the rocker cover. I took Martins (from local club) advice and re-torqued the head, this time to 55lb ft. As I believe BMC has said here, the manuals are wrong its not 40lb-ft for an A series engine but 55lb-ft. Those with Mini experience know this.
Did this, then re-torqued to 55 and the leak dissapeared!
Strange as I've got away with 40lb/ft a few times before.
Posted: Wed Jun 28, 2006 10:14 am
by Kevin
the manuals are wrong its not 40lb-ft for an A series engine but 55lb-ft.
Well I find it strange that the original BMC manuals are wrong but I will check as I have one, I can understand the haynes style ones being incorrect as they often seem to have some facts wrong, but I find it hard to believe the factory ones are wrong as the A series was in production for many years before the mini came along and I would have thought that an extra 30% increase on the studs would not be ideal, could them problems be caused but studs & nuts pass their sell by dates.
I am sure Ray can add more technical detail to this issue.
Posted: Wed Jun 28, 2006 12:03 pm
by RogerRust
I think the higher torque is for studs ith a drill point marking or the number 22 on the top. as per the studs on the 1275 Sprite.
Standard ones are 40 ft pounds
Don't try and over do it they strip very easily
Posted: Wed Jun 28, 2006 11:40 pm
by Kevin
Thats right roger so unless the stronger studs are fitted your are right about the risk.
Still not sorted my head as we couldnt get workshop access

fingers crossed for tomorrow

Posted: Thu Jun 29, 2006 11:04 pm
by Kevin
Its starting to look a bit doubtful for Alfie

, I hope I dont have to come in modern metal
But all the best to those who are setting off tomorrow and I will see you on Sunday one way or the other

Posted: Fri Jun 30, 2006 8:25 am
by chickenjohn
No problem with the slightly higher torque on my car! It has fixed the slight leak.
40lb/ft is not actually that tight.
I've heard some folk say that higher torque values are needed these days as the head gaskets are not as good as they used to be, or the manual is wrong and the mistake was copied.
Posted: Fri Jun 30, 2006 9:45 am
by chrisd87
I did mine to 45lbs, didn't seem especially tight but I really don't want to risk a snapped stud!