Is it catching
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- Minor Addict
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That's rather uncanny - my bypass hose sprang a leak just after I had the head off a few days ago. Got a couple of new ones - 95p from the local MG Rover dealer! 

[img]http://i31.photobucket.com/albums/c390/chrisd87/DSC00749.jpg[/img][img]http://i31.photobucket.com/albums/c390/chrisd87/med_gallery_128_45_1416415.jpg[/img]
Sarah - 1970 Minor 1000 2-dr
Maggie - 1969 Minor 1000 4-dr
Sarah - 1970 Minor 1000 2-dr
Maggie - 1969 Minor 1000 4-dr
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Use a piece of heater hose its what was used originally and lasts far far longer than the bellows type. and I wish it was just the bypass hose that was my problem rather than the bypass tube .Got a couple of new ones - 95p from the local MG Rover dealer
Cheers
Kevin
Lovejoy 1968 Smoke Grey Traveller (gone to a new home after13 years)
Herts Branch Member
Moderator MMOC 44706
Kevin
Lovejoy 1968 Smoke Grey Traveller (gone to a new home after13 years)
Herts Branch Member
Moderator MMOC 44706
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- Minor Addict
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- Joined: Mon Nov 07, 2005 4:52 pm
- Location: Saffron Walden
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I would have used a piece of heater hose if I'd known it was dodgy when I had the head off, but only when I'd put it back on did it start leaking 

[img]http://i31.photobucket.com/albums/c390/chrisd87/DSC00749.jpg[/img][img]http://i31.photobucket.com/albums/c390/chrisd87/med_gallery_128_45_1416415.jpg[/img]
Sarah - 1970 Minor 1000 2-dr
Maggie - 1969 Minor 1000 4-dr
Sarah - 1970 Minor 1000 2-dr
Maggie - 1969 Minor 1000 4-dr
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- Moderator
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Yes thats it on the underside of the head.Bypass tube?
Do you mean the outlet the bypass hose attaches to?
Hmm sorry but that sounds a bit of a bodge to me.
It might be ok as an emergency fix but with whats left of mine which is just a rusty serrated piece less than a third of its original length, I would rather it was done properly and what probably caused it was not running with a decent antifreeze mixture all year round some time in the past.
Cheers
Kevin
Lovejoy 1968 Smoke Grey Traveller (gone to a new home after13 years)
Herts Branch Member
Moderator MMOC 44706
Kevin
Lovejoy 1968 Smoke Grey Traveller (gone to a new home after13 years)
Herts Branch Member
Moderator MMOC 44706
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- Minor Legend
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Leaving the egg jokes aside (didn't Leonard Lord describe the Morris Minor as looking like a poached egg???)- back to head gaskets-
after doing a blown exhaust valve in Jan, the traveller ran very well but some oil crept into the water and a small amount of mayonnaise on the rocker cover. I took Martins (from local club) advice and re-torqued the head, this time to 55lb ft. As I believe BMC has said here, the manuals are wrong its not 40lb-ft for an A series engine but 55lb-ft. Those with Mini experience know this.
Did this, then re-torqued to 55 and the leak dissapeared!
Strange as I've got away with 40lb/ft a few times before.
after doing a blown exhaust valve in Jan, the traveller ran very well but some oil crept into the water and a small amount of mayonnaise on the rocker cover. I took Martins (from local club) advice and re-torqued the head, this time to 55lb ft. As I believe BMC has said here, the manuals are wrong its not 40lb-ft for an A series engine but 55lb-ft. Those with Mini experience know this.
Did this, then re-torqued to 55 and the leak dissapeared!
Strange as I've got away with 40lb/ft a few times before.
Cheers John - all comments IMHO
- Come to this years Kent branches Hop rally! http://www.kenthop.co.uk
(check out the East Kent branch website http://www.ekmm.co.uk )


- Come to this years Kent branches Hop rally! http://www.kenthop.co.uk
(check out the East Kent branch website http://www.ekmm.co.uk )

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Well I find it strange that the original BMC manuals are wrong but I will check as I have one, I can understand the haynes style ones being incorrect as they often seem to have some facts wrong, but I find it hard to believe the factory ones are wrong as the A series was in production for many years before the mini came along and I would have thought that an extra 30% increase on the studs would not be ideal, could them problems be caused but studs & nuts pass their sell by dates.the manuals are wrong its not 40lb-ft for an A series engine but 55lb-ft.
I am sure Ray can add more technical detail to this issue.
Cheers
Kevin
Lovejoy 1968 Smoke Grey Traveller (gone to a new home after13 years)
Herts Branch Member
Moderator MMOC 44706
Kevin
Lovejoy 1968 Smoke Grey Traveller (gone to a new home after13 years)
Herts Branch Member
Moderator MMOC 44706
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- Minor Legend
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I think the higher torque is for studs ith a drill point marking or the number 22 on the top. as per the studs on the 1275 Sprite.
Standard ones are 40 ft pounds
Don't try and over do it they strip very easily
Standard ones are 40 ft pounds
Don't try and over do it they strip very easily

This message board is like a family - you can't choose the other members!! But remember engine oil is thicker than water.
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Its starting to look a bit doubtful for Alfie
, I hope I dont have to come in modern metal
But all the best to those who are setting off tomorrow and I will see you on Sunday one way or the other


But all the best to those who are setting off tomorrow and I will see you on Sunday one way or the other

Cheers
Kevin
Lovejoy 1968 Smoke Grey Traveller (gone to a new home after13 years)
Herts Branch Member
Moderator MMOC 44706
Kevin
Lovejoy 1968 Smoke Grey Traveller (gone to a new home after13 years)
Herts Branch Member
Moderator MMOC 44706
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- Minor Legend
- Posts: 4064
- Joined: Tue Dec 07, 2004 8:50 am
- Location: Margate, East Kent
- MMOC Member: No
No problem with the slightly higher torque on my car! It has fixed the slight leak.
40lb/ft is not actually that tight.
I've heard some folk say that higher torque values are needed these days as the head gaskets are not as good as they used to be, or the manual is wrong and the mistake was copied.
40lb/ft is not actually that tight.
I've heard some folk say that higher torque values are needed these days as the head gaskets are not as good as they used to be, or the manual is wrong and the mistake was copied.
Cheers John - all comments IMHO
- Come to this years Kent branches Hop rally! http://www.kenthop.co.uk
(check out the East Kent branch website http://www.ekmm.co.uk )


- Come to this years Kent branches Hop rally! http://www.kenthop.co.uk
(check out the East Kent branch website http://www.ekmm.co.uk )

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- Minor Addict
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I did mine to 45lbs, didn't seem especially tight but I really don't want to risk a snapped stud!
[img]http://i31.photobucket.com/albums/c390/chrisd87/DSC00749.jpg[/img][img]http://i31.photobucket.com/albums/c390/chrisd87/med_gallery_128_45_1416415.jpg[/img]
Sarah - 1970 Minor 1000 2-dr
Maggie - 1969 Minor 1000 4-dr
Sarah - 1970 Minor 1000 2-dr
Maggie - 1969 Minor 1000 4-dr