Tuned the mixture a flat leaner. Took the Moggy for 10km cruising run. Great ride and noticeable power increase. Overtook couple of Ashok Leyland buses

Realizing that I've been running on just three cylinders all this time blaming it on the engine and perhaps thinking that the timing was too retarded. Only now I'm experiencing the true power of 948cc BMC A series engine

2016 seems to have started showing prosperity..

Thinking of inspecting the plugs after a while for the so called "biscuit tan"
I wouldn't suspect the piston rings / bore right now unless the new plug in cylinder 4 gives up again after a while under the new mixture setting. Probably a dodgy plug running on a rich mixture caused all the trouble.